Upgrading the Wabeco F1210 -- Adding DROs for all axes

Retrofitting a vertical mill with digital radouts (DROs) significantly expedites machining. The attachment brackets for the digital calipers were easily machined. A large LED display improves readability. 

To prevent chips from falling onto the horizontal calipers, I protected these with a polycarbonate cover.
Since the rotary table handle was touching the cover, I had to elevate the rotary table by adding a baseplate.


The digital calipers worked very nicely. I just did not keep them for very long, because they became redundant and had to go when I upgraded the mill to CNC.

Upgrading the  Wabeco F1210 -  Servo control retrofit (CNC, all axes)

In the past, I had attempted to attach stepper motors to my old Rotwerk milling machine for a CNC retrofit. I got the X and Y  axes to work, but had to give up on the Z axis. 

The photos below document how involved such an upgrade can get.

In the past, I had attempted to attach stepper motors to my old Rotwerk milling machine for a CNC retrofit. I got the X and Y  axes to work, but had to give up on the Z axis. 

The photos below document how involved such an upgrade can get.

To start out, I had to disassemble the entire mill, which required several modifications because I wanted to replace the trapezoidal screws by ball screws. A member of the German CNC forum offered to help -- his help was really appreciated. The above photograph shows the vertical column of my mill precisely aligned on the T-table of a "real" milling machine which is shown milling a sufficiently large slot to take up the ball screw nut.


Both sides of each ball screw required machining: I first center-drilled and bored them on the lathe so that I could insert the  original end pieces, anchoring them with metal adhesive. I later realized that this appraoch was not satisfactory. Bonding was not the issue -- it was adequate, but the preload of the thrust bearings could not be adjusted because the bearing preload is set against the timing belt pulley, the bushing of which cannot take up the load. Incorrect distances to the attachment points made me add spacer blocks to the ball screw nuts.


There is not a lot of space left -- the clearance for the new ballscrews would not have been sufficient if we had not enlarged the slot. Isel does not sell wiper kits for the X axis ball screw nuts. Yet retrofitting wipers is straightforward: Just machine a pair of mounts. I drilled the original nuts to be able to push in insert nuts, which I anchored with a metal adhesive.


The servomotors were retrofitted with encoders, replacing the resolvers. For this, the motors had to be disassembled. In order to not demagnetize the magnets, it is of utmost importance to insert a suitable iron tube into the field frame while the armature is being extracted. 


All motors are mounted. The picture also shows the respective enclosures for the timing pulleys and couplings.


A couple of electronic boards for the UHU servo controller need to be soldered, a manual control has to built.... and the CNC mill is ready to run.


Home and limit switches are essential: The motors are quite powerful and would possibly damage the machine if they were to overrun the limits of the axes.
When I had finished machining the first couple of workpieces, an increasing amount of backlash became noticeable on the X and Y axis. The cause was quickly located: The thrust bearings had become loose because the bushings supporting the timing  belt pulleys could not take up the load.


These are the new thrust bearings with ZKLN axial angular contact ball bearings preloaded inside the enclosure by a nut. After this modifications, the timing belt pulleyonly has to transfer radial forces.  


The ways were beginning to show signs of wear, and wear translated into less positional accuracy on the XY table. I re-scraped the ways to make the entire surface take up the load instead of just the edges. Several channels can be seen on the bottom of the T-table; the purpose of these channels escapes me. These channels contribute to uneven wear on the opposite side. I filled the channels with metal and metal polymer, added a coating of Moglice and re-scraped these surfaces as well. The table moves now much more smoothly and evenly.


As a last modification to the Wabeco milling machine, I added a secondary high speed spindle. With a power of 200 W and an rpm of 17500, the spindle is quite suitable for engraving work.
 

back